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authorBin Liu <b-liu@ti.com>2024-10-31 12:23:15 -0500
committerGreg Kroah-Hartman <gregkh@linuxfoundation.org>2024-12-05 10:59:40 +0100
commitde350906dc3ab562c94f7d548afc034a9a8c8b25 (patch)
tree9bc00adca937f6b429a33206122da56361001fea
parentb174ab33aaafd556a1ead72fa8e35d70b6fb1e39 (diff)
downloadlinux-stable-de350906dc3ab562c94f7d548afc034a9a8c8b25.tar.gz
linux-stable-de350906dc3ab562c94f7d548afc034a9a8c8b25.zip
serial: 8250: omap: Move pm_runtime_get_sync
commit bcc7ba668818dcadd2f1db66b39ed860a63ecf97 upstream. Currently in omap_8250_shutdown, the dma->rx_running flag is set to zero in omap_8250_rx_dma_flush. Next pm_runtime_get_sync is called, which is a runtime resume call stack which can re-set the flag. When the call omap_8250_shutdown returns, the flag is expected to be UN-SET, but this is not the case. This is causing issues the next time UART is re-opened and omap_8250_rx_dma is called. Fix by moving pm_runtime_get_sync before the omap_8250_rx_dma_flush. cc: stable@vger.kernel.org Fixes: 0e31c8d173ab ("tty: serial: 8250_omap: add custom DMA-RX callback") Signed-off-by: Bin Liu <b-liu@ti.com> [Judith: Add commit message] Signed-off-by: Judith Mendez <jm@ti.com> Reviewed-by: Kevin Hilman <khilman@baylibre.com> Tested-by: Kevin Hilman <khilman@baylibre.com> Link: https://lore.kernel.org/r/20241031172315.453750-1-jm@ti.com Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
-rw-r--r--drivers/tty/serial/8250/8250_omap.c4
1 files changed, 2 insertions, 2 deletions
diff --git a/drivers/tty/serial/8250/8250_omap.c b/drivers/tty/serial/8250/8250_omap.c
index b9352d3bb2ed..77bef81488f2 100644
--- a/drivers/tty/serial/8250/8250_omap.c
+++ b/drivers/tty/serial/8250/8250_omap.c
@@ -643,12 +643,12 @@ static void omap_8250_shutdown(struct uart_port *port)
struct uart_8250_port *up = up_to_u8250p(port);
struct omap8250_priv *priv = port->private_data;
+ pm_runtime_get_sync(port->dev);
+
flush_work(&priv->qos_work);
if (up->dma)
omap_8250_rx_dma_flush(up);
- pm_runtime_get_sync(port->dev);
-
serial_out(up, UART_OMAP_WER, 0);
up->ier = 0;